WE Report

Lessons Learned

Lessons Learned865


Operator Rig Discipline / Origin Project Phase Well Section Date What Happened

DNO
2004 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
P&A 27/07/2021
Franks tong was moved into the drill floor from the starboard tool landing are on the skate through . . .

Drilling Supervisor / Stig Seland



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DNO
1994 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-1 H
Oselvar
P&A 21/07/2021 Bottom 0.5 m of the toolstring is the Ultrasonic rotating IBCS-E sub. This sub has a larger OD . . .

Drilling Supervisor / Stig Seland



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DNO
1993 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-1 H
Oselvar
P&A 19/07/2021 Jacked 9 5/8″ free using Baker Mastodon jacking tool. Used 49 pressure cycles to jack casing 17 m, . . .

Drilling Supervisor / Stig Seland



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DNO
1990 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-3 HT2
Oselvar
P&A 13/07/2021 Set 20″ EZSV at 694,5 m according to procedure. Tagged EZSV with 10 t. Pressured up to 50 bar, no . . .

Drilling Supervisor / Stig Seland



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DNO
1991 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-3 HT2
Oselvar
P&A 13/07/2021 Pulled pack off assembly free. Flow checked well. Pulled MPT with pack off assembly above BOP. . . .

Drilling Supervisor / Stig Seland



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DNO
1970 – DNO

Borgland Dolphin Drilling Operational A-3 HT2
Oselvar
P&A 05/07/2021 The 9 5/8″ casing hanger had a 10″ pup joint made up to it This was not identified on the hanger . . .

Drilling Engineer / Stig Seland



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DNO
1969 – DNO

Borgland Dolphin Drilling Operational A-1 H, A-2 H, A-3 HT2
Oselvar
P&A 01/07/2021
Drill crew observed that Slips for perforating guns came out
to rig without handles.

Øystein Prytz / Stig Seland



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DNO
1968 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
P&A 30/06/2021 Initially believed that we did not get a good pressure test (Formation Integrity Test). Suspected . . .

Drilling Supervisor / Stig Seland



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DNO
1930 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
P&A 29/06/2021 We had a lot of friction in a long and deviated well A3 with brine.

Drilling Supervisor / Stig Seland



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DNO
1554 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
P&A 03/06/2021 Overtorqued connection required cold cutting

Drilling Supervisor / Stig Seland



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DNO
1547 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
N/A 29/05/2021 Camera not able to get a 360 view as it was off center

Lars Solvang / Stig Seland



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DNO
1456 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-3 HT2
Oselvar
P&A 03/05/2021 Both sides of the UHG can be used on the TRT but the port side of the UHG comes into conflict with . . .

Drilling Supervisor / Stig Seland



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DNO
1457 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-3 HT2
Oselvar
P&A 03/05/2021 Concerns were raised that with the HXT landed on the 105 ton skid as planned the bumper bars on the . . .

Drilling Supervisor / Stig Seland



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DNO
1446 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-3 HT2
Oselvar
P&A 26/04/2021 A week’s work trying to pull completion, high overpulls throughout, over 200 plastic clamps lost . . .

Drilling Supervisor / Stig Seland



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DNO
1425 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-3 HT2
Oselvar
P&A 20/04/2021
Total planned well volume was 150 m3 (tubing 50 m3, annulus 100 m3). After pumping 81 m3 the rig . . .

Drilling Supervisor / Stig Seland



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DNO
1426 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-3 HT2
Oselvar
P&A 20/04/2021
Evaluated rig-up and HXT valve and BOP status. Changed HXT valve status to the following: opened LPR . . .

Drilling Supervisor / Stig Seland



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DNO
1427 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-3 HT2
Oselvar
P&A 20/04/2021
Optimised process as follows:
Lined up rig BOP Lower Kill line to rig choke manifold and . . .

Drilling Supervisor / Stig Seland



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DNO
1428 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-3 HT2
Oselvar
P&A 20/04/2021
Ran tubing cutter in one assembly to avoid arming tool after assembling in sections.
Near perfect . . .

Drilling Supervisor / Stig Seland



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DNO
1429 – DNO

Borgland Dolphin Drilling Operational A-3 HT2
Oselvar
P&A 20/04/2021 Operations completed successfully, but forgot to flush lines from SFT to bleed-off package with . . .

Drilling Supervisor / Stig Seland



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DNO
1419 – DNO

Borgland Dolphin Drilling
Own Experience
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
P&A 11/04/2021 We pressure tested the BOP in an untraditional way using a BOP jump tool. This took very long time . . .

Drilling Supervisor / Stig Seland



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